Re-cast the part again today to try a few more changes:
First change, built a new cope 2" deep in place of the older one 3.5" deep.
Second change, increased the size of the riser from 1.25" dia to 1.5" dia
Third change, increased the size of the well under the 1" sprue to 1.5 dia
Fourth change, made the path of the gates more square than curved
Fifth change, dusted the mold cavity with plumbago
Total furnace melt time from lighting to pour 1:15
Diesel fuel used: 1.25 gal
Results were a general further improvement over the last pour. Finish was greatly improved, though corners were more rounded (result of blacking). There were still a couple of minor holes, though they looked like they would be removed when the surfaces were machined, and the channel bored to 1" dia.
The main problem that came up was again my mis-estimate of the amount of slag/vs metal in the pot, and a nearly short pour as a result. I did not fill the sprue and riser completely, though they filled sufficiently to make a good casting.
I really need to slag out the crucible while in the furnace, rather than out, so I can get a better visual take on the amount of metal in the pot -- and can add more if needed. The slag is very puffy so it takes up a lot of space. The slag used to appear much smaller when I used a flux which liquified it. Now it's got the appearance of cottage cheese. Last pour I scraped it in the furnace and added more metal -- there was plenty for the pour. This time I didn't scrape it beforehand and assumed I had enough metal.
I had no trouble with the shallower cope, and I think it is going to be an improvement. I think the riser and gating were good, except that the gates could have been bigger -- the pour went unusually slowly. Possibly because of the lower head pressure of the thinner cope. I think a completed pour with more metal might have made a very good part.
