Steps forward...... Steps backward. But, overall......

Mounted the original c/i piston, on a handy piece of curtain pole, and reduced to fit the new bore.
About -5thou from original.......

Assembled. But couldn't get the engine to
spin freely. Seems the open end of the bore is a little tight.

So...... Turned another length of curtain pole, to a sliding fit. (After sanding off the fuzz)........

Coated in fine grinding paste. And oscillated for 30mins, or so.......

Seems Dave has gripped on the end of the cylinder o/d, in his industrial machine, and triangulated it!

Re assembled, again. Piston/ bore, dry, no oil. shouldn't pick up. Just a quick test run.
Twin temporary burners, this time.......
Now, I'm confident to carry on modding, to finish, as planned.

Except......
An hour after running. The piston was stuck in the bore. Again!
The dreaded, condensation rust.........

Sheesh........

Pleased, the lap is still mounted in the chuck. I can polish the bore, for the new graphite piston.
Winter's closing in, on old bones. Not much will be happening this week.
Thanks for looking in!
David D