My lathe (10 x 22 import) has a 1 3/4 in. x 8 tpi spindle. It came with a three jaw chuck and a 6 in. 4 jaw chuck seen here:
chuck backplateNote that the backplates have threaded holes to match with two locking devices that can be used to prevent the chuck from screwing off the spindle. It also came with a faceplate - not shown.
I also have a new 5 in. 4 jaw chuck that requires a backplate. This chuck is lighter and more useful for smaller jobs than the 6 in. chuck so I decided recently to get at making a back plate.
Spindle:
chuck backplateLast week I picked up a piece of ductile iron - 6 in. in diameter and about 1.5 in. thick. I also had on hand a pieces of 2.5 in. diameter hot rolled steel rod.
chuck backplateA couple of days ago I started to make a fake spindle with the threads and shoulder. The existing spindle was measured for diameter and length.
I cleaned off the outside of the hot rolled steel with a steel brush and got it running as true as I could in the 3 jaw chuck. The outboard end was faced and drilled with a centre drill so that a live centre would give it support.
chuck backplate(not sure if this is proper procedure but it seems to work).
The diameter of the shoulder is a bit greater than the threaded portion so I turned the full length to that diameter first. The threaded portion was then turned down just under 1.75 in. and a cut taken at the back of the threads with a cut off tool - to provide and "ending" on each threading pass.
A 60 deg. hss threading tool was set up and I threaded the majority of the thread depth under power. It is a bit tricky with this lathe as the slowest speed is about 150 rpm. Once it was nearing proper depth I first used a thread guage then used the faceplate and 4 jaw chuck to test the fit. Nearing the end my "threading mandrel" was installed and I completed the threading turning the spindle by hand.
At one point I thought I had the threads correct and dismantled my threading setup. The threading was found to be too shallow and I had to pick up the thread again. Being that the threads were 8 per inch it wasn't too difficult.
The final result can be seen below:
chuck backplateToday I installed the piece of ductile iron close to centre in the 6 in. four jaw and faced both sides. It had been cut on an industrial bandsaw but was still out some so it took a while and worked the lathe pretty hard.
Further to come although it may be a while as I will take my time with this.
John.