Gallery, Projects and General > Oooops!
Stuck Collet Chuck Arbor
Fergus OMore:
I think that we have to thank our Rob and DoubleBoost for reminding me of perhaps the simplest solution.
Simply turn a metal dowel to a fairly tight fit in the top of the hollow spindle. Find a suitable bottle cork( Happy Birthday, Rob) and fill the hollow spindle to the top with hydraulic oil( Thanks John- Andy Barton and so on) Insert the cork, follow up with the tight fitting dowel-- and hit it. :hammer:
It's boring, it's ancient and despite all the so called expert criticism, it actually works. It is a crude hydraulic jack.
doubleboost:
I remember using this method to remove spigot shaft bearings from morris 1000s :) :) :)
We used to pack the bearing with grease put a old first motion shaft in the hole and whack the bugger
I would not like to think of the pressure generated but it worked :lol: :lol: :lol: :lol:
John
Fergus OMore:
Yes, John,
I did say that the male lot of my family were all blacksmiths. :hammer:
Your idea is splendid. If the poor wee soul has been pouring WD-40 and summat called Kroil- whatever that is, down the lot, there will be sweet nothin' left in the ball races. Grease, what a good idea :beer: Re-pack the bearings. Unusual but heigh ho-- I like it. :clap: :clap: :clap:
Fergus OMore:
Whilst Rome wasn't built in a day, there should be progress with the chuck by now.
Don't keep us in suspense :bow: :hammer:
ukazak:
well,
it has been more than ten days now, machine is running without the drawbar. at least 4hrs a day, up hill, down hill, fast and slow, with fly cutting, slot cutting and 16mm end mills and all... nothing hapened so far. running just as usuall. ıt just doesnt give..
unal
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