Hi
I have been working on this for weeks and finally after a long day sitting at the computer screen

I got the motor up and running for one axis. The aims was just to get one axis going and then finally with that confidence, complete the project. CNC interested me from the beginning so it has always been on the cards and the redundancy of my little lathe due to the arrival of the boxford had left a perfect opportunity.
The hardware:
4 wire bipolar Nema23 - 270 oz/inch, 2.8A not a huge amount of muscle but big enough I should think for one of the axis on this mini lathe
Routout CNC Bipolar driver board 2.5A
Standard 25 way breakout board
18-20V 3.5A Laptop Charger that I had lying around the house with no use.
Software: Mach 3
So some of you may notice that the driver doesn`t actually power the motor to the maximum but seeking advice from a few people, I was advised that for the extra cost of the 10A driver boards, the 0.3A would be virtually unnoticeable and certainly not worth the extra money for this test. The guys at Routout CNC were excellent and a few phone calls to them have helped me no end. Here is a piccy of the lathe with the computer in the background (perhaps should have tidied up!):

This is the driver, motor and BOB connected:

At this point I could confirm that the driver was engaging the motor as when powered, the motor was locking up. However I spent ages trying to setup and correctly configure the software to actually move the motors. For future reference if this helps anyone, here are some screen shots of the critical settings in Mach3:




My first attempt at a bit of simple G-code which worked and turned the motor "forward" 0.5 inch!

So now I have my motor turning under CNC and next is a case of correctly hooking it upto my lathe. I bought quite a few bits off Lee and so the Y axis should be quite straight forward. The first job however is going to be the tailstock - the motor is mounted but the motor centre spindle is turning in the connector block so here is the thing dismantled and next job is to drill and tap the connector lower down so that the grub screw correctly engages and locks with the motor spindle.

Hopefully I should make some more progress over the next few days.
Chris