Hi all,
Finally got in the garage and did something, although nothing exciting like the start of building a new model, essential work nevertheless!
When I bought my Harrison lathe about a year ago, the only thing I could fault was the 3 jaw chuck. It was old and worn, hence didn't run true any more. This was frustrating as I had just sold a couple of good chucks on ebay

always the way isn't it! I put up with it for a while but recently decided to get a new one from Axminster (I had bought an Axminster one for my previous lathe and found it to be good).
So a few weeks back I decided to try and fit it, at which point I couldn't get the chuck undone ... it had obviously been on there for years and tightened itself on over that period of time. Some of you might have seen my post when I was trying to get it off, having broken gears etc!

Anyway, it came off in the end, that's the main thing.
Before I start I should say that this is not intended to be a 'how to guide' but is simply the way I tackled the job and it worked for me.
Spindle with chuck removed:
Fitting New Chuck to LatheGave it a clean and applied some grease:
Fitting New Chuck to LatheCleaning thread on chuck backplate:
Fitting New Chuck to LatheNew chuck:
Fitting New Chuck to LatheChecking size of register on new chuck, the sizes are in metric and the hole is 95mm diameter!
Fitting New Chuck to LatheThought I better measure that for real, not that I don't trust them or anything you understand

Fitting New Chuck to LatheChecking the size of the existing backplate shoulder to see how much I need to remove:
Fitting New Chuck to LatheTaking a skim off the shoulder to ensure everything is running true:
Fitting New Chuck to LatheWasn't too happy with this finish .. I knew I was using a tool with the wrong rake angle really though
Fitting New Chuck to LatheSo I ground up a new tool and increased the speed slightly, this is better (I can't engage the power feed since I crunched my change wheel!)
Fitting New Chuck to LatheNext I worked out what I needed to take off the shoulder, luckily it was bigger than the register in the new chuck so I didn't have to start from scratch, just had to make it smaller diameter. I converted the amount needed to take off into imperial

so I could use the handwheels on the lathe.
I initially went 0.10mm oversize then kept trying the chuck taking cuts of 1/2 a thou off:
Fitting New Chuck to LatheBingo, a the chuck is a good snug fit on the shoulder as can be seen by the fact it's staying there by itself! I shouldn't have taken that pic, it could have fallen onto the lathe bed ... knowing my luck the camera would have taken the pic at the point of impact!!

Luckily it didn't fall!
Fitting New Chuck to LatheNow I had to skim the face on the back plate where the back face of the chuck fits to ensure that was running true, I was careful not to take too much off, otherwise the shoulder could become too deep:
Fitting New Chuck to LatheChecking the depth of the register in the new chuck, the leaflet said 3mm, think it was 3.3 or something.
Fitting New Chuck to LatheChecking that the depth of the shoulder is less than the register, you can see daylight, so it's smaller.
Fitting New Chuck to LatheNext I had to mark out the 3 mounting holes in the right places. This is the method I used, put a centre in the headstock taper and set the cutting tool inline with it.
Fitting New Chuck to LatheThe spec said 108mm PCD for the mounting holes so a quick

revealed that I needed to wind the cutting tool 2.126" back. (I double checked the PCD with a vernier and it was near enough right.) With the spindle running slowly I touched the sharp corner of the cutting tool onto the backplate scribing a line all the way around at 108mm PCD.
Fitting New Chuck to LatheHere you can see the scribed line:
Fitting New Chuck to LatheI then thought, how am I going to get the 3 holes equispaced 120 degrees apart?! Well I'd done this before, I don't know why I removed the back plate from the spindle, it needed to stay on there. I used the holes that were already drilled in the back plate to get my 120 degree offsets. I lined one of the existing holes up with a mark on the head stock by eye with the aid of a straight edge (cutting tool). This could have been improved by putting something through the hole I guess ... just thought of that though! Anyway, once lined up I scribed a short line with the cutting tool intersecting the 108 PCD line. This was then repeated with the other 2 holes.
Fitting New Chuck to LatheNext, the holes had to be centre punched, centre drilled and opened up to 8mm clearance.
Fitting New Chuck to Lathe
Fitting New Chuck to Lathe
Fitting New Chuck to LatheTaking the burrs of with needle file, don't get much burr drilling cast iron:
Fitting New Chuck to LatheTapping the backplate onto the chuck ensuring it's driven fully home:
Fitting New Chuck to LatheTightening in the allen bolts a bit at a time, pulling the chuck up nice and square against the face:
Fitting New Chuck to LatheChuck fitted with a bit of grease in the jaws etc.
Fitting New Chuck to LatheAll that was left was to turn the OD of the backplate to match the chuck ... probably unnecessary really.
Fitting New Chuck to LatheThe finished job:
Fitting New Chuck to LatheActually, I found the motion of the jaws really tight so decided to take it back off. Took the cover off the back and the insides were bone dry

Is it meant to be like this? I thought not so put some grease in there! That probably wasn't what was causing the friction though, there are 3 screws that hold cover plate on and it seems if they are too tight the whole motion locks up. Wondered why they weren't tight. This seems the same on the pratt & bernard chuck that I took off too.
Fitting New Chuck to LatheThat's about it really. I haven't really tried it out yet but I did put a DTI on the chuck body and an end mill gripped in the jaws. There was 0.02mm runout on the chuck body and between 0.02-0.03mm on the end mill. More than good enough for me, and not bad for £45!
Fitting New Chuck to Lathe
Fitting New Chuck to Lathe
Fitting New Chuck to LatheNext job is to try it out and make a special bush for the gear that will replace the one I smashed! Then onto a proper project, possibly with a house move in between!
