Gallery, Projects and General > Project Logs
Another Paddleducks build log
<< < (61/70) > >>
sbwhart:
 :offtopic:

Got this one from Aldi a few weeks ago £12.50 with lots of bits, 240V nice a chunky with plenty of humph, at that price you can risk nackering it up as a tool post grinder.



Stew
spuddevans:
My "dremel" is in fact the Axminster version, and I was going to try using the flexible extension part of the kit as it is only about 3/4" thick ( or there-abouts ) and hopefully relatively easy to mount to the toolpost.

I figure that even though the bearings may not be rated for this sort of application, it will not be seeing much use, I intend to turn down using conventional methods until I get really close, and then I will grind only the 2 3mm sections after hogging out the middle section. That being the ( theretical ) case I dont see too much wear if I take it really easy. ( famous last words ), and even if it does cause any damage, the damage will be to the flexable extension and not to the tool itself.

But like I said, I'll have another search in the metal stocks to see if I can find the 6mm silver steel,  hopefully I will find it.


Tim
NickG:
Stew I got that one from Aldi about 6 months ago - same price!
spuddevans:
Well, talk about resurrecting an old topic :bugeye: I cant believe that it has been over 4 months since I posted any updates.

Due to my better half's health situation, until recently I havent been able to spend much more than 20mins at a time in the workshop, which meant I hadnt made much progress on this build ( or on much else ). But things seem to have settled a bit to allow me a bit more time in the 'shop so I thought I'd update this build log.

To date I have remade one (already remade :bang: ) piston valve and made a new steam chest for it and succeeded in keeping a much closer fit.

I also have modified the pistons to accept o-rings.

I then started to chase down and fix as many causes of friction that I could.

I bored the bearing blocks all the way through, they originally had a 5mm thru hole for the crankshaft, and a 8mm diameter pocket each side for the ball races. I have since found that there was some friction being caused by the 5mm sections, so I got all 4 bearing block bored out to 7.8mm in the mill, then I carefully alligned them all together in the vice and used a 8mm hand reamer to open them out the final 0.2mm. Then I stuck some 8mm silver steel rod thru the 4 and gave them all a wipe over some 600grit w&d on a surface plate.

Then I loosely assembled the bearing blocks onto the baseplate, stuck the 8mm rod thru them, and then tightened them up. Then I lapped them using the same 8mm silver steel rod and some T-cut to get them spot on. Then I re-assembled the crankshaft with all the ball races and the difference was unbelievable, silky smooth and free.

After re-assembling the whole engine and re-timing it I applied some air to it and........





It ran  :D :D :D :D  ( for about 20 secs until my little airbrush compressors tank was empty )


It seems to be quite an air-hog at the moment. I got it started on 50psi and it ran until the tank got down to about 25-30psi. I havent got any gasketing installed at the moment, nor any stuffing in the glands, so that will be my next process, chasing down the air leaks.

I also have noticed that there is a lot of air that seems to going straight thru the valving to the exhaust without meeting the piston, so that too will have to be investigated.

Overall I am quite pleased that I have got it to run on my little compressor, previously it had not had enough stored air to turn it over more than a couple of revolutions.


So while it is taking me ( quite ) a while, it is satisfying that at least there is some progress to report, hopefully in the coming weeks I will be able to post up a video of it working.


Tim
sbwhart:
Hi Tim

Pleased that things are settling down for you, and that you've had some success with the engine, look forward to seeing the video.

Stew
Navigation
Message Index
Next page
Previous page

Go to full version