Preliminary woodwork is done:
It's bit bumpy on the edge contour part, and will be taken care of at the stage, when the body is to be prepared for painting. At least there is now more room to move the tremolo away from the string retainer, as long as the fork of it doesn't interfere with the spring.
When thinking about the guitar bodies(and some furnitures), that I've painted in the past, they are far from good. Not that the looks is that important, but what can one expect, when painting with a brush, using thick paint.
For once, it would be nice to have a smooth, evenly painted surface.
Ordinary spray paint cans, available from hardware stores, have quite limited colour scale. The colour, or say, kind of colour, that I'm after, is subtly translucent, like when looking at tomato. It is neither plain red, nor plain orange. Closest acrylic colours are cinnabar or vermilion, but nah, they are still flat colours.
Anyways, small airbrush, although I have never used one, may be a considerable option. Good ones are pricey for occasional use, so why not make one. There are plenty of Youtube videos, where they use components/parts, that I already have. As long as it's simple, and doesn't spit, I'm in.
I have a small compressor, that doesn't have a tank, but few big, interconnected soda bottles can be used to beef up its 'breathing capacity'.
So, exploring the ways, of how to combine colours, and test the techniques, is a subject for a (possibly)forthcoming side-project of its own.
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I managed to make almost straight hole, without breaking the 1.5mm drill bit:
First I drilled as deep as possible, and at the end, there was only 2 or 3mm of the drill bit length in the chuck. Very slow and tedious thing to do, as this kind of aluminum tends to stick to the flutes of the drill bit, and cause notorious 'snap'. Without having any proper cutting fluid, I applied some beeswax to the flutes often. Don't know how or why it works, but the thing that matters, is the end result.
The straight part of the hole itself is a bit loose for 1.5mm rod. When drilling from the other end, it went off by a small amount, as I expected. That eccentricity between the holes, after all, seems to be a good thing, as now that rod have to be tapped, or pressed to get it through, keeping it firmly in place.
Hard to say at this point, if that's the case, after the slots for rollers are machined. If the hole is still too loose after that, then other tricks like tinning the rod, will be used.