It's been awhile since I threaded in the lathe. Like maybe 3 years. And an inside bore Acme 1/2" screw is not a favorite threading task. So I renewed the joys of searching for the right change gears, squinting to try to read the layout chart on the inside cover of the gear housing, getting blackened grease on arms, clothes and, as I discovered later at my family's surprised smiles, face.

With the gears finally set up properly, I pulled out the pin in the bull gear, flipped the gear engagement lever, checked for proper carriage travel direction, set the compound to 14 degrees with a magnifying glass, and loosened and engaged the thread dial with the leadscrew. I checked that the tool was square to travel, moved the cutter to the bore start, zeroed the two slide dials, and finally started a cut.
Well, things were going okay, at the the lowest speed the Craftsman was capable of. I was starting to think I hadn't lost the touch. The only problem was, I hadn't figured out what the compound's depth of cut should be for a 10TPI Acme thread at 14-/2 degrees compound. But Being the try and fit type, I did have my somewhat wounded tap, which I'd ground back a little, and I figured I would just test the bore periodically with that. Once it was close, I could use the undamaged part of the tap to make the final cut.
Things went well and the tap showed promise of getting near to the end of lathe threading. I was able to screw it in 1, then 2, then 3 turns with the lathe stopped. I kept working it in, and then backing off, gaining ground bit by bit, though it seemed to be getting tighter. But I felt the end was in sight so I applied a little more pressure -- not enough to break anything, but definitely putting some pressure on. It moved a little when I bumped it with my hand, but it never seemed to break through.
Then I noticed I was turning the whole workpiece in the chuck jaws. I guess I hadn't tightened those enough to resist this kind of mistreatment. So I was well, screwed ......again. The tap couldn't cut it, and now the threads were out of register with the lathe threading dial. I did the usual mistaken last hope in this situation -- trying to re-align the tool and slides and threading dial while taking the backlash out of the gear train. But as usual, all I managed to do was mess up the threads.
Time for a break!
